中国塑料 ›› 2018, Vol. 32 ›› Issue (02): 27-32.DOI: 10.19491/j.issn.1001-9278.2018.02.004

• 材料与性能 • 上一篇    下一篇

聚丙烯/丁烷挤出发泡工艺参数的优化

王泽鸣1,汪澎2,信春玲3,何亚东3   

  1. 1. 北京化工大学机电工程学院
    2. 泰信塑料有限公司
    3. 北京化工大学
  • 收稿日期:2017-08-22 修回日期:2017-09-26 出版日期:2018-02-26 发布日期:2018-02-26
  • 基金资助:
    国家重点研发计划

Optimization of Extrusion Process Parameters of Polypropylene with Butane Gas

  • Received:2017-08-22 Revised:2017-09-26 Online:2018-02-26 Published:2018-02-26

摘要: 采用正交实验设计法对聚丙烯(PP)/丁烷挤出发泡的工艺参数(成核剂添加量、注气量及机头压力)进行了研究,通过扫描电子显微镜,得到了不同工艺条件下的泡孔结构,并借此分析了各工艺参数对材料发泡倍率、平均泡孔直径和泡孔密度的影响程度及机理;进一步利用Design Expert软件对PP的发泡工艺进行了优化,并通过实验验证了优化工艺的预测值。结果表明,在成核剂用量为1.4 %、机头压力为4.66 MPa、发泡剂注入量为7 %时,材料的发泡倍率高、泡孔密度大、泡孔直径小;通过实验验证,实验结果与预测值的偏差小于5 %,证明了预测的可靠性。

Abstract: Extrusion foaming parameters (i.e. nucleating agent, gas injection and die pressure) of PP with butane gas were investigated by an orthogonal experimental method. Cell structures obtained under different process conditions were determined by scanning electron microscopy. The effects of process parameters on the expansion ratio, average cell diameter and cell density of PP foams were analyzed, and the relevant mechanisms were discussed. The foaming process was further optimized with the Design Expert software, and the resulting process parameters were confirmed by the relevant experiments. The results indicated that the PP foams achieved a high expansion ratio, a high cell density and a large average cell diameter when the content of nucleating agent, die pressure and gas injection amount were set to 1.4 wt %, 4.66 MPa and 7 %, respectively. The experimental results also verified the theoretical predication with a deviation lower than 5 %.

中图分类号: